What Is A Pressure Tank? Why Do You Need It?
When a house is built in an area that is not served by a
municipal water works, a private well system is used. The well pumps
used in most systems are quite powerful, often capable of delivering
more gallons of water per minute than any single faucet could draw.
Everybody I have spoken to in the plumbing or water-well business
says that well pumps can burn out prematurely if they are made to
start and stop more than necessary. By using a holding tank, the
water can be used in a leisurely manner over a long time, and the
pump will run briefly to refill the tank.
A pressure tank can be as simple as a big metal chamber with one
hole in the bottom for water to flow into. As the pump pushes water
in, the air in the tank is compressed. At some point, called the
cut-out pressure, a switch interrupts the power to the pump and no
more water enters the tank. Since there is compressed air above the
water, there is enough force acting on the liquid to push it out of
the tank, through the pipes, and all the way upstairs (possibly
several flights of stairs) to the faucet.
But... there is a flaw with this simple design. Air can be
dissolved in water, believe it or not. Eventually a simple tank with
compressed air above the water will experience a loss of this
compressed air. So the air space above the water gets smaller day by
day. What you notice is that the pump will run for very short
periods, perhaps 5 or 10 seconds, and do this frequently whenever
water is being drawn.
That is exactly what was happening in my own home. The remedy is
simple: just add more air to the tank with an air compressor. For
years I have been doing this about every 2 months. It only takes a
couple of minutes, but it's still a maintenance chore. Besides,
there's a better way.
A proper well pressure tank does not use a simple empty steel
can, it uses a flexible bladder or bag inside the tank, with the
bottom of the bag pointing to the bottom of the tank. The bladder
occupies a portion of the total tank volume. The steel tank contains
compressed air. The operation is the same as the plain tank example
above, but the bladder keeps the water separated from the air. The
air never meets the water, so the air does not become dissolved in
the water. The tank never needs to be charged with air, unless
the fill valve (which is like a tire valve) leaks.
But... eventually the bladder can leak. After all, it flexes
every time the water is used, so wear and tear is expected. Once the
bladder leaks, the tank reverts to a plain style of pressure tank
(with a ripped rubber bag inside), so the compressed air slowly
bleeds out. Plus you can get chunks of rubber in your water lines,
which has its own set of problems.
That is why we replaced our pressure tank. Simple
wear-and-tear.
But on this job I had a skilled helper: my good friend Tommy
Skusa, a licensed plumber with 17 years of experience in all sorts
of residential, commercial and industrial projects. I let Tommy do
most of the work, while I took some pictures and tried to stay out
of the way.
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The old pressure tank. |
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| This is the Schrader valve used to add air
to the upper part of the tank. |
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These two photos show the tank and control apparatus, and the
pipe that enters the house from the well. Note there is also a wire
that leads to the well.
As you can see, all this plumbing is under the basement stairs,
so it made for crowded working conditions and less-than-perfect
pictures.
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I turned off the breaker that supplies the
well pump.
This is a 240-volt breaker, which is common for well
pumps. |
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| Tommy drained the system with a short
piece of hose and a bucket. This took about 5 minutes. |
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He removed the plastic cap covering the
pressure switch. |
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| I removed the wires. The outer wires were
the supply lines.
Being a 240 volt device, both lines are
switched. So this is a 2-pole switch. |
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The inner two wires go to the pump.
I removed these carefully because it was obvious that
they were quite old wires. That cloth wrapping was used
a long time ago, I would guess this was installed in the
late 1950's or early 60's. The lack of a ground wire
also dates the wire. I understand that by 1964 grounded
wiring was required by the National Electrical Code. |
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| I removed the cable clamps too. They
weren't holding very well. |
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The pressure switch after being
disconnected. |
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| We loosened the the dielectric union that
connected the newer copper main pipe to the older
galvanized steel pipe.
All of these pipes here are one inch diameter. |
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Tommy used a pair of pipe wrenches to
loosen the union fitting in the line between the well
and the tank. |
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| He disconnected the union while holding up
the pipe, so it would not tip the tank over. |
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Tommy just twisted the tank around and
walked it out of its hiding spot beneath the stairs... |
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| ... and then set it on a workbench so we
could dismantle the old parts.
The tank didn't weigh much... maybe 25 pounds with
all those extra pipe fittings. |
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After removing the pressure switch (it sat
on a ¼" nipple, about 4 inches long) we removed
the pressure gauge with a crescent wrench. This was also
a ¼" fitting |
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| We removed the boiler drain valve, and we
unscrewed the pipe that fed into the multi-port well
tank fitting. |
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We tipped the old tank over. |
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| We carefully removed this section of pipe
from the old tank, because I wanted to save the tank for
possible use with compressed air. |
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Reconnecting the pressure switch:
Tommy wrapped the ¼" nipple with Teflon tape.
Note the direction of wrap. When the pipe is screwed in,
the tape won't be peeled back.
It's important to use Teflon tape at the pressure
switch connection, because paste thread compound can
break away and gum up the switch. |
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It's a good idea to replace the simple rubber diaphragm in the
pressure switch at this time, but we forgot about that and it's a
long way to the hardware store. So we re-used the old switch as-was.
| He installed a new pressure gauge, being
careful not to overtighten and strip the ¼"
threads... |
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... and he replaced the pressure switch |
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Note that the multi-hole fitting has been cleaned up. I took it
out to the shop and used my buffer (a bench-grinder-mounted wire
wheel) to remove some of the dirt and rust. This can also be done
with a wire brush, but that is slow and tedious.
Apparently this piece was not galvanized. I also cleaned up the
drain valve.
| With the tank gone from the corner, I took
a minute to clean out the debris that had fallen from
the stone rubble foundation. |
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I cut off the 1 inch supply pipe that
leads from the tank to the rest of the house. Since the
new tank is much wider than the old one, the pipes will
need to be moved a bit. |
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| Tommy assembled this section of piping and
carefully screwed it into the new pressure tank. The
black part on the bottom of the tank is a plastic
fitting, which made Tommy kinda uneasy. But I think the
plastic is glass-filled nylon, which is really tough.
Still, he didn't want to over-tighten the connection
and strip the plastic threads, causing a big delay in
getting the water restored. |
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We put a few pieces of pipe together to
see what would be the best route to the tank from the
old pipe |
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| Take 2:
We tried a different approach, going away from the
wall on a 45° angle and then turning.
Note how this new lateral pipe turns downward before
entering the tank. We had to do this because the new
tank was farther from the wall than the old tank, and we
needed a vertical pipe to connect to the copper pipe
above. |
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We placed the tank on a pair of 4"
cement blocks.
I wanted the tank to be higher off the ground than
the previous one, so I could get a pail under the drain
valve
I have seen many instances of pressure tanks sitting
on the basement floor, and having great difficulty
draining the system for repairs because the drain valve
was only a half-inch above the floor.
Using a dinner plate to drain a tank is not a quick
process. But that's what you do when you forget to bring
a piece of garden hose. |
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| Tommy likes to make sure his supply pipes
are nice and level. I've never seen any other plumber do
this. But Tommy's work looks good... and functions well
too.
This is a plumber who carefully lays out his supply
pipes, snapping chalk lines and keeping hot and cold
lines perfectly parallel at 8 inches apart. And level
too, or a slight slope towards a drainage point.
Pride in workmanship. Now that's cool. |
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I reconnected the wires at the pressure
switch.
The pump wires (red arrows) did not instill
confidence, but I connected them anyway, since replacing
the wire in the middle of winter, under four feet of
frozen ground, is not gonna happen.
First I installed new cable clamps because the old
ones were messed up.
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| I connected the supply wires to the outer
terminals. There is not much room under the cover of
this electrical junction box.
I was leery of the insulation cracking and crumbling
on those old wires, so I kept the bending and flexing to
a minimum. |
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Tommy reconnected the copper line. |
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| The one-inch main pipe runs just over head
at this point... |
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... and comes from the dielectric union
just downstream from the pressure tank. |
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When the copper pipe was finally reconnected, and the wiring to
the pressure switch was done, we closed the main ball valve (visible
in the photo above) and turned on the pump breaker.
Since there was no pressure at the switch, the contacts were
closed, and the pump started right away. The pressure tank filled up
and the pump shut off. The clicking of the pressure switch is quite
audible, and the action of the pressure gauge also tells what is
happening.
Then I slowly opened the main shut off valve. Water filled the
pipes and was visible in the swirl-down clear-bowl filter nearby.
But then... the needle on the pressure gauge fell to zero and
stayed there. What the...?
It Didn't Work!
I took the cover off the pressure switch. It was still closed, as
it should be.
Using a non-contact voltage detector I probed for power at the
wire that runs from the switch to the pump. The sensor beeped,
indicating power.
I was stumped. Maybe the pump took a dump? But Tommy
noticed something.
| The photo at right shows the pressure
switch when it is OPEN, that is, the pressure in the
tank is high, has reached the "cut-out" point,
and the pump is not needed.
The red arrows point to the two brass conductive
connectors. At each end of these is a round dot of metal
(bronze, perhaps) that touch opposing round dots, when
the switch closes. |
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These round dots are the contacts, and they take a lot of
abuse. Whenever the contacts open (as the pressure reaches the upper
limit) there is the visible flash of arcing current. Like miniature
lightning. This arcing creates heat and oxidizes the metal. Most
metal oxides are not good conductors.
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The pressure switch when closed, when the
pressure in the tank has dropped to the
"cut-in" point and the switch now energizes
the pump.
Notice how the opposing contacts are now touching,
creating a path for current to flow. |
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What Tommy noticed was a tiny bit of oxidation on the contacts,
visible as a light-colored surface.
The solution was simple: I got a little
strip of emery cloth and folded it lengthwise to form a
double-sided abrasive strip.
- I manually opened the switch
- I slipped the emery cloth between the contacts
- I let the switch snap shut
- I simply pulled the strip out.
I did this 4 or 5 times for each of the 4 pairs of
contacts. (Of course I turned the power off) |
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I turned the power back on and the pump worked fine.
But why did the voltage sensor detect power and the pump not run?
One wire must have been energized, and the other dead. It
only takes a break in one of the two wires to interrupt
power to the device... but for reasons of safety 240 volt well
pump pressure switches are double-pole switches, interrupting both
wires.
Why: Because residential 240 volt systems employ two
hot wires. One wire is 120 volts higher potential than ground,
and the other wire is 120 volts lower potential than ground.
The potential difference (also called voltage) between
the two hot wires is 240 volts.
Remember - just because a 240 volt device is not running
doesn't mean there is no power to it. You can still get
shocked if one line is live. |
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The completed installation. Sort of.
The wiring to this system is a big 'ol code
violation. These cables need to be inside conduit,
either rigid or flexible.
But I will be rebuilding the stairs in the future, and at that time I will also be correcting the
gaggle of poor wiring in this area. |
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This is a Sears Craftsman Captive Air® tank, model 390.291658,
which is a 36 gallon tank. The label says it is equivalent to an 82
gallon standard tank.
This tank has a replaceable bladder, which should save money in
the long run as complete tank replacement would not be necessary.
But bladder replacement involves draining the system and removing
the tank. The air valve can also be replaced... it is an ordinary
car tire valve.
With cut-in/cut-out settings of 40 and 60 PSI, this tank has a
draw-down of 9.3 gallons. That means that I can draw over 9 gallons
of water before the pump will kick on. We were experiencing the pump
turning on once every time a 3.5 gallon toilet was flushed, and when
the air got low the pump would kick in 3 or 4 times per flush.
Now I hardly ever hear the pump turn on.