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| In
This Article:
The torn fiberglass screen is
removed from a storm door and replaced with new screen and
spline material. |
Related
Articles:
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| Skill Level:
1-2 |
Time Taken:
1 Hour |
By
Bruce W. Maki,
Editor
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This storm door screen was splattered with paint
and had a long gash that was patched with a sewn-on piece of
screen fabric. |
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The black rubber strip (called a spline)
holds the screen into the frame.
I used a screwdriver to pry up the end. I found it easiest
to work on a rug on the floor.
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Once the spline was pried up I simply pulled it
out of the groove. This screen has four spring-loaded catches
that hold the frame into the door.
The spline had been cut at each catch, so I used a
scratch-awl to pick at the end and pry it up.
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Same as before... pry the end up and pull the
spline from the groove. |
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The previous installer must have inserted the
catch pins after the screen was put in. Most window screens
don't have these little catch mechanisms. This one took some
careful prying to get apart. |
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The metal pins were removed.
The old screen was simply pulled up from the frame.
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I bought a 25 foot roll of fiberglass screening because I
have several screens to make. Smaller rolls are available at
not much of a savings.
I unrolled the new screening next to the old piece, and cut
the mesh about 1/2 inch longer. |
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There are two common diameters of spline material, .175"
and .125". This is the larger size. Luckily it fits
the groove in the old frame.
Note the ribs around the spline. These probably keep the
spline in place. |
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I left about 1/4" overlap on the first corner.
The spline roller is used to push the rubber spline
into the groove. |
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The spline roller looks like a double-ended pizza cutter.
One roller has a groove. This end is used the most.
This tool costs about $2.50 at Home Depot. |
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After the first corner is anchored,
the opposite end of the screening is pulled taut to prevent
waviness in the finished job. |
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The spline is laid out along the first groove and then
pushed into place with the roller.
I had the best results when I used two hands on the roller.
It takes a fair amount of force to push the spline into the
groove. |
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At the end of the first stretch, I used a flat
screwdriver to push the spline into the corner. |
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I looks like I might have cut the screening too small.
Once the spline was inserted up the the second corner I
realized that I did have enough screen (but barely). |
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Now the screen is pulled across the frame and
held in place (with my knee) while the spline is pressed in
place. |
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The spline is in place on all four sides.
A sharp knife is used to cut the spline. |
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The pizza roller is used to finish inserting the spline.
Notice the slight warp to the long side of the frame. The
tightness of the screen may have flexed the frame into an hourglass
shape. |
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I'll ignore the warped frame and continue. The excess is
trimmed off with a sharp knife.
The finished product. I would be done if the screen had no
special pins for holding it in place. |
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I've never dealt with these little pins before.
I pried up the spline at the pin hole and cut a small section
out. |
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The pin is inserted. There is a tiny coil spring
inside the frame. One of them was dislodged in all the
handling, but I was able to find it by sticking my awl into
the hole and tilting the screen until the little rascal slid
down. |
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The little plastic sleeve is pressed onto the pin.
The spline is pressed back in place with a screwdriver. |
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Ummm... Ooops!! The screen frame fits tight at
the top, but in the middle it is too narrow!
The gap is just a bit too big to keep out bugs. (I
didn't claim to be an expert, did I ?)
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So, I took the screen back out and removed only the
two pieces of spline in the middle of the long frame rails.
(Because of the cuts made for the hold-in pins, the spline is
now in segments.) I carefully straightened the aluminum frame
tubing.
Whew! There was just enough screen to fit. After my first
attempt the frame was about 1/2" narrower in the middle
than the top or bottom. |
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The splines were re-installed, with a lot less tightness to
the screening material. The frame ended up being about
1/8" narrower in the middle. The gap at left is good
enough for me.
The finished product looks much better than before. Total
time, including fixing my goof-up, was under an hour. |
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Tools
Used:
- Screwdriver, Flat Blade
- Scratch-Awl
- Sharp Knife
- Scissors
- Screen Spline Tool
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Materials Used and Cost:
- Screening - $1.20
- Spline - $0.50
- Total - $1.70
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Copyright © 1999-2003
HammerZone.com
Written May 6, 1999
Reformatted February 4, 2003
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